Any chance of you / EMC doing a write up of this mod in the newsletter or the forum?
Gavin suggested to drill a Pilot hole up through the centre of the strut rod bracket and right through into the diff. Make sure you have a container ready ! I thought I would get through the bracket then the dif, they must be touching as when I broke through I realised I had gone through both as oil started coming out. ( I put some grease on the drill bit to catch any swarf) when the oil has all drained the next thing to do is enlarge the pilot hole in the bracket Only, using a 1” hole saw. ( Be very careful here only to enlarge the hole in the bracket) de burgh the edges.
Once the bracket hole is clear, step by step enlarge the pilot hole in the diff casing up to the11.8mm tapping size drill. Now take your 1/4 Bsp t(taper) tap. I couldnt use a tap holder due to the exhausts so found a socket that fitted the square shaft of the tap. It took a while for the tap to start to bite as the tap is very fine at the tip. It finally started to cut , again, I put some grease on the tap to catch swarf or chips of diff casing.
Trickiest part was keeping the tap going up straight as you are working arms up in the air and very achey. Half turn forward , quarter turn back. Due to the thin case of the diff you are only cutting one or two threads, the ta then stops cutting and just runs up through the thread into the diff. This is as much as you can do.,
I then wiggled a magnectic screwdriver around in the hole and picked up a few more metal chips. I then flushed a pint of ordinary gearbox oil through to flush out any other debris.
I left it overnight to fully drain and then re filled with the correct ac delco oil and additive. I put in one quart of oil then added the additive then topped up with the other quart of oil until it just ran out of the fill plug. It looked to have sealed but notice one drip had formed overnight. I was very cautious not to over tighten due to the few number of threads. I tightened a bit more , checked next day, one drip , re tightened and seemed drip free. Ibthen took car to a car park and drove several slow figure of eights as I read that this would dstribute the oil and additive throughout the plates of the posi drive.
Next morning ,… One Drip !!

ffs so back on the ramp, drained the diff , ( a doddle with the new plug) caught and saved every drop of the 95 quid amber nectar. Added a copper crush washer and some ptfe tape to the plug. Tightened up tighter than before , re filled it and it finally seems drip free.
So to run through requirements ,
You will need ,
A 1/4 inch bspt plug ideally allen headed but mine had a 16mm hex head.
A pilot drill aprox 1/4 inch.
I hole saw approx 1 inch.
A 1/4 bspt tap (taper, not parallel) .
An 11.6 or 11.8 drill (tapping size) for bsp tap and a few drills between that and the pilot drill to open up the pilot hole ready to tap . . Hope this explains in detail. Good luck.
